Jump to content

Powervalve stuck? after topend rebuild


Recommended Posts

Did a top end today on a 250 xcw tpi.  I cleaned the cylinder with carb cleaner before reassembling. The powervalve wasn't dirty at all to begin with so I didnt tear it apart apart from getting access to the bolt under the cover.  I did spray a bunch of carb cleaner on it though, and on the other side where the other cylinder bolt is located.  I threw some oil on everything when reassembling but now the clawed powervalve assembly unit is kinda stuck in the raised position.  I need to lower it so I can reattatch the powervalve ball joint and close it up.  Did I screw something up or do I need to finesse it to move up and down freely.  I didnt mess with anything in there aside from carb cleaner spray. 

Also- the indexing pins are not letting the newly purchased Slavens S3 mule head seat completely on the cylinder.  They are properly indexed but not seating flush.  Is it a machining issue with the head, or should I just cinch it down with the head bolts? Maybe the piston is too high, but it looks just about flush with the top of the sleeve. EDIT- there is a rubber o-ring in between the head insert and the inside of the head.  Im thinking im assembling this right so maybe the oring just needs to be smushed down.....or maybe i have the oring in the wrong spot, thus raising the head off the cylinder 1.5mm

Edited by N.dica
Link to comment
Share on other sites

To help anyone who might have a similar problem:

I hadnt disassembled the entire powervalve because the outer housings were pretty clean and muck free.  But, since I had to open up the powervalve to get what was stuck unstuck I found out that the inside of the powervalve had a considerable amount of carbon buildup that was undetectable without disassembly. Good lesson here- clean out your powervalve with a piston swap and keep things running fresh.  Id imagine that a fair amount of poorly performing engines are the result of needing a good cleaning.  I only had 65 hours on mine, but it was a lot of slow technical enduro riding so that contributed to the carbon buildup.  Now that it is clean, everything is operating smoothly without a hiccup.

Also, in response to my piston head fitment, I think I was sent a mislabeled 300 head instead of a 250 head.  Waiting til monday to confirm.

Edited by N.dica
Link to comment
Share on other sites

Create an account or sign in to comment

You need to be a member in order to leave a comment

Reply with:

×
×
  • Create New...