I did the de-smog/de-baffle/rejet today. Seems to run correctly now.

I still have the stock air-cleaner/pipe at this point. I ran a #52 pilot (#55 back ordered), #158 main, needle shimmed .022, slide drilled

The bike has 300 miles on it and was getting 50 mpg mostly freeway.

It's now 56 mpg and I sure will improve as it racks up some more miles.

It is no longer cold blooded, which I knew the jetting would fix.

It also runs about 20 degrees cooler overall.


Create an account or sign in to comment

You need to be a member in order to leave a comment

Create an account

Sign up for a new account in our community. It's easy!

Register a new account

Sign in

Already have an account? Sign in here.

Sign In Now